Noon Patrol test pilot Jerry Stevens reports on engine teardown.
Wed Jun 12, 2002 3:25 pm

The engine was taken down by the NTSB and the FAA. There was
galling on pistons number 4 and 3 near the top. This was believed
to have happened during the prop strikes on the ground as none of
the particles had made it to the oil screen or were found in the
lower end. There was a broken compression ring on #3 and may have
happened when installed. Oil was found in both 3 and 4 but it was
not burned and was probably introduced when the aircraft was upside
down and the oil was allowed to drain from the blowby to the carb
and then when uprighted it drained through the carb and into the
intake on cylinder number 4 mostly and some in number 3. We also
found oil in the intakes on that side as well. The engine was turned
over by hand after the crash and that is when the oil got in the
cylinder. There was no oil down the belly so this didn't happen in
flight and no smoke was seen by anyone at any time.

The only thing that was found was that the distributor was not
tightened back up after it was timed. It could be easily moved by
hand. With the engine running and setting the timing you would not
want to tighten the stop nut down until it was turned off. As they
say shit happens. There will be a red line drawn on the side of our
distributors, after they have been properly tightened and safety wired,
to show the proper location of the distributor to the housing from
this point on.

It doesn't look like it will take too long to get this one ready to
fly again. The lower wing will not take long to fix. The engine will
have to be put back together and some new parts added as well. The
lower longeron will not be a difficult fix. The upper wing bow will
be easy as well. We have an extra set of gear legs already. Build
one rudder and we will be on our way.

Jerry (The lowest time nieuport pilot on the planet. 20 min)